[1]朱苏青,李 兴,李景辉.陈堡油田油井自转向酸化解堵试验研究[J].复杂油气藏,2017,(01):69.[doi:10.16181/j.cnki.fzyqc.2017.01.014]
 Zhu Suqing,Li Xing,Li Jinghui.Study on plugging removal by self-diverting acidization for Chenbao Oilfield[J].Complex Hydrocarbon Reservoirs,2017,(01):69.[doi:10.16181/j.cnki.fzyqc.2017.01.014]
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陈堡油田油井自转向酸化解堵试验研究
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《复杂油气藏》[ISSN:1674-4667/CN:31-2019/TQ]

卷:
期数:
2017年01期
页码:
69
栏目:
油气工程
出版日期:
2017-03-25

文章信息/Info

Title:
Study on plugging removal by self-diverting acidization for Chenbao Oilfield
作者:
朱苏青李 兴李景辉
中国石化江苏油田分公司采油一厂,江苏 扬州 225265
Author(s):
Zhu SuqingLi XingLi Jinghui
No.1 Oil Production Plant of Jiangsu Oilfield Company,SINOPEC,Yangzhou 225265,China
关键词:
自转向酸化 表面活性剂 性能评价 现场试验 陈堡油田
Keywords:
self-diverting acidizing surfactant property evaluation field test Chenbao Oilfield
分类号:
TE39
DOI:
10.16181/j.cnki.fzyqc.2017.01.014
文献标志码:
A
摘要:
针对陈堡油田供液变差井酸化改善效果有限的问题,采用自转向酸酸化技术以实现酸化过程中酸液自动转向和深部穿透的目的,且酸化后遇烃自动破胶,返排彻底,无二次伤害,可以高效、均匀地酸化储层。通过缩合反应和季铵化反应合成出了一种具有自转向性能的粘弹性表面活性剂,并通过实验评价了浓度、pH值、温度等因素对该自转向剂粘度的影响。优选陈堡油田主力单元水平井进行自转向酸化解堵试验,取得很好的增油效果。
Abstract:
To solve the problem of limited effect in conventional acidizing for wells with low fluid production in Chenbao Oilfield,the self-diverting acidization technology was proposed.The self-diverting acid fluid can automatically redirect and penetrate deeply target layers in the process of acidizing.The gelatinous self-diverting acid can be broken by contacting hydrocarbon after acidizing.And then the reacted acid can flow back easily without residuals and secondary damage.As a result,the target formation can be homogeneously and effectively acidized by the self-diverting acidization technology.A kind of viscoelastic surfactant with self-diverting property was developed through condensation reaction and quaterisation reaction.It was carried out evaluation on the effect of concentration,pH value and temperature on the viscosity of self-diverting acid fluid.The technology was implemented in horizontal well in Chenbao Oilfield.The obvious oil increasing oil effect was obtained.

参考文献/References:

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备注/Memo

备注/Memo:
收稿日期:2016-06-24; 改回日期:2016-09-07。
作者简介:朱苏青(1972—),硕士,高级工程师,现从事采油工程研究与管理工作。电话:0514-86763505,E-mail:zhusuq.jsyt@sinopec.com。
更新日期/Last Update: 2017-03-25