[1]陈晓宇,姜宇玲,李 牧,等.泡排辅助增压开采工艺应用效果分析[J].复杂油气藏,2020,13(03):77-80.[doi:10.16181/j.cnki.fzyqc.2020.03.016]
CHEN Xiaoyu,JIANG Yuling,LI Mu,et al.Analysis of application effect of foam drainage assisted pressurized mining technology[J].Complex Hydrocarbon Reservoirs,2020,13(03):77-80.[doi:10.16181/j.cnki.fzyqc.2020.03.016]
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泡排辅助增压开采工艺应用效果分析()
《复杂油气藏》[ISSN:1674-4667/CN:31-2019/TQ]
- 卷:
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13卷
- 期数:
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2020年03期
- 页码:
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77-80
- 栏目:
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油气工程
- 出版日期:
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2020-09-25
文章信息/Info
- Title:
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Analysis of application effect of foam drainage assisted pressurized mining technology
- 作者:
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陈晓宇1; 姜宇玲2; 李 牧1; 李凌君1; 杜家澄1
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1. 中石化重庆涪陵页岩气勘探开发有限公司,重庆 408014;2. 中国石化江汉油田勘探开发研究院,湖北 武汉 430223
- Author(s):
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CHEN Xiaoyu1; JIANG Yuling2; LI Mu1; LI Lingjun1; DU Jiacheng1
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1.Sinopec Chongqing Fuling Shale Gas Exploration and Development Co.,Ltd.,Chongqing 408014,China;2. Exploration and Development Research Institute,Sinopec Jianghan Oilfield Company,Wuhan 430223,China
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- 关键词:
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天然气开发; 泡沫排水采气; 增压开采
- Keywords:
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natural gas development; foam drainage gas recovery; pressurized mining
- 分类号:
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TE377
- DOI:
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10.16181/j.cnki.fzyqc.2020.03.016
- 文献标志码:
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A
- 摘要:
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针对M区块部分气井增压效果变差的问题,开展泡沫排水采气工艺辅助增压开采试验研究。通过改进泡排流程及起泡剂用量优化调整,经现场应用,试验气井稳产、增产、助排效果显著,优化后的单井雾化消泡流程现场效果较好。试验表明,起泡剂加注量应实行一井一制,根据实际情况不断调整优化。
- Abstract:
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Aiming at the problem of poor pressurization effect of some gas wells in M Block,the foam drainage gas recovery process was used to assist pressurized mining. By improving the foaming drainage process and optimizing the amount of foaming agent,the test gas wells had a significant effect on stable production,increasing production,and drainage assistance.The optimized single well atomization defoaming process had a good field effect. Test results have shown that the amount of foaming agent should be one well for one strategy,and continuously adjusted and optimized according to actual conditions.
参考文献/References:
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备注/Memo
- 备注/Memo:
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收稿日期:2020-07-22;改回日期:2020-07-26。第一作者简介:陈晓宇(1989—),助理工程师,从事采气工艺、动态监测管理等方面的工作。E-mail:393755765@qq.com。基金项目:国家科技重大专项“涪陵页岩气开发示范工程”(2016ZX05060)
更新日期/Last Update:
2020-09-30